![]() |
If this is your first visit, be sure to check out the FAQ by clicking the link above. You may have to register before you can post: click the register link above to proceed. To start viewing messages, select the forum that you want to visit from the selection below. |
|
|
Thread Tools | Display Modes |
#1
|
|||
|
|||
![]()
The faceplate on my Narco CP-136 Audio Panel was broken off (and glued back
together) before I bought the plane. The left side of the faceplate, where 2 retaining screws attach it to the metal chassis, had been glued at least once before I bought it, and my avionics shop had glued it back together for me twice. All to no avail. In extreme cold, the glue would simply let go. There simply wasn't enough original plastic left for the epoxy glue to grip. So, when I picked up my plane from its recent transponder installation, I was not surprised when the faceplate suddenly popped out on the left side during the climb-out. (Hey -- everything in the panel had actually WORKED as advertised for a good 2 minutes! :-) Vowing to somehow permanently fix the damned thing, I jumped on line when I got home... Suffice it to say that the alternatives I found were not good. The cheapest solution I found was a used unit for $175 on Ebay. Narco wanted $200 (!) for just the faceplate. At that point, I knew it was worth taking some time and thinking this thing through -- so I pulled the audio panel out of my minus 10 degree hangar and took it home to warm up in my workshop. After raising it almost 80 degrees to room temperature, I carefully removed the screws from the remnants of the original plastic. It was obvious that some meathead had yanked it out -- hard -- by the faceplate, in an attempt to remove it from the panel. They probably didn't realize that the installation allen screw on this unit was the kind that you could turn forever, until it literally backed the unit right out of the panel. (Some radios just have allen screws that lock or release the unit from the panel, which results in you having to then slide them out "manually" with a yank or two.) After too many gluings, the plastic around the screws was just a mess. When I backed the screws out, the piece literally crumbled, leaving nothing left to glue. I now had a rectangular faceplate with NOTHING at one end to screw through. (For a visual image of this, imagine a shoe-box lid with one end cut off...) Now what? With nothing to lose, I wrapped the end of the faceplate with a piece of strapping tape -- the only thing I could think of that would be strong enough, yet removable. I then C-clamped the faceplate on end, so that the missing end was flat on my work-bench. I then started mixing up a batch of J-B Weld... J-B Weld is a 2-part mixture, rather like a thick epoxy except that it applies like a "flowing" putty. It fills large voids, dries without expanding (or contracting) into a rock-hard texture, and can be drilled, cut and sanded. I carefully spooned my first batch into the void framed by the strapping tape and the sides of the faceplate, making sure it was in contact with the sides and back without over-flowing anywhere, and let it dry over night. The next day the new part looked good (better than expected, as it had "gravity-smoothed" perfectly) and was well adhered to the sides -- my faceplate had an "end" again! Still, it was a bit thin, and I didn't want to take the chance of it breaking when I tried drilling it. So, another batch of goop was mixed up, and I carefully built up another layer, packing it in but again making sure not to over flow the edge of the tape... Next morning it looked much more stout, but -- since the weather was absolute crap anyway -- I mixed up another batch and used it to reinforce the OTHER end, so it wouldn't break off someday, too. I also packed some into the corners of the piece (using a toothpick) to reinforce some stress points, and filled in a couple of cracked areas from behind while I was at it. This was tedious, as the pieces are small, and you have to be careful not to add material to spots that need to clear certain parts. (Like the light bulbs for the marker beacon lights...) The following afternoon it was time for the big test -- could I actually drill this stuff without breaking the new "end" out completely? I first carefully removed the strapping tape, and was surprised when it came off of the new material rather easily. I then marked where the holes needed to go, chucked the piece on end into my drill press, and EVER so carefully lowered the spinning bit into the new plastic. You can imagine how relieved I was to find that it cut through just fine. The new J-B Weld plastic was just as strong (maybe stronger?) than the original part, and I quickly finished drilling both holes. It was a little spooky counter-sinking the holes for the screw heads, since it meant hitting the piece with a fairly large drill bit. Again, however, it held up to the drilling force just fine. Upon reassembly, however, I discovered that my new end was JUST a tad thicker than the original -- I had reinforced it a bit much. This didn't allow the faceplate to mount on the audio panel chassis properly, so, using the spinning bit in my drill press like a router, I carefully hogged out tiny bits of the new material at a time, until it fit perfectly. All that was left was the cosmetic touches. Using some flat black model paint (J-B weld dries to a light gray color), I painted the new material to match the original plastic. Since the repair is almost entirely on the side of the faceplate, it's nearly impossible to see the new piece, and -- after painting to match -- you can't see it at all. I reinstalled the unit today, and it fits, looks, and works as good as new. J-B weld is amazing stuff, and I'm $200 ahead because of it. -- Jay Honeck Iowa City, IA Pathfinder N56993 www.AlexisParkInn.com "Your Aviation Destination" |
#2
|
|||
|
|||
![]()
On Sun, 01 Feb 2004 21:57:29 GMT, "Jay Honeck"
wrote: snip I reinstalled the unit today, and it fits, looks, and works as good as new. J-B weld is amazing stuff, and I'm $200 ahead because of it. Now invest some of that money in a Dremel tool and I'd bet you'll be able to literally sculpt your next J-B Weld project. Don |
#3
|
|||
|
|||
![]()
"Sharpie" brand permanent markers make excellent "touch-up" tools for
most black instrument surfaces. Much easier than painting. Rip Jay Honeck wrote: The faceplate on my Narco CP-136 Audio Panel was broken off (and glued back together) before I bought the plane. The left side of the faceplate, where 2 retaining screws attach it to the metal chassis, had been glued at least once before I bought it, and my avionics shop had glued it back together for me twice. All to no avail. In extreme cold, the glue would simply let go. There simply wasn't enough original plastic left for the epoxy glue to grip. So, when I picked up my plane from its recent transponder installation, I was not surprised when the faceplate suddenly popped out on the left side during the climb-out. (Hey -- everything in the panel had actually WORKED as advertised for a good 2 minutes! :-) Vowing to somehow permanently fix the damned thing, I jumped on line when I got home... Suffice it to say that the alternatives I found were not good. The cheapest solution I found was a used unit for $175 on Ebay. Narco wanted $200 (!) for just the faceplate. At that point, I knew it was worth taking some time and thinking this thing through -- so I pulled the audio panel out of my minus 10 degree hangar and took it home to warm up in my workshop. After raising it almost 80 degrees to room temperature, I carefully removed the screws from the remnants of the original plastic. It was obvious that some meathead had yanked it out -- hard -- by the faceplate, in an attempt to remove it from the panel. They probably didn't realize that the installation allen screw on this unit was the kind that you could turn forever, until it literally backed the unit right out of the panel. (Some radios just have allen screws that lock or release the unit from the panel, which results in you having to then slide them out "manually" with a yank or two.) After too many gluings, the plastic around the screws was just a mess. When I backed the screws out, the piece literally crumbled, leaving nothing left to glue. I now had a rectangular faceplate with NOTHING at one end to screw through. (For a visual image of this, imagine a shoe-box lid with one end cut off...) Now what? With nothing to lose, I wrapped the end of the faceplate with a piece of strapping tape -- the only thing I could think of that would be strong enough, yet removable. I then C-clamped the faceplate on end, so that the missing end was flat on my work-bench. I then started mixing up a batch of J-B Weld... J-B Weld is a 2-part mixture, rather like a thick epoxy except that it applies like a "flowing" putty. It fills large voids, dries without expanding (or contracting) into a rock-hard texture, and can be drilled, cut and sanded. I carefully spooned my first batch into the void framed by the strapping tape and the sides of the faceplate, making sure it was in contact with the sides and back without over-flowing anywhere, and let it dry over night. The next day the new part looked good (better than expected, as it had "gravity-smoothed" perfectly) and was well adhered to the sides -- my faceplate had an "end" again! Still, it was a bit thin, and I didn't want to take the chance of it breaking when I tried drilling it. So, another batch of goop was mixed up, and I carefully built up another layer, packing it in but again making sure not to over flow the edge of the tape... Next morning it looked much more stout, but -- since the weather was absolute crap anyway -- I mixed up another batch and used it to reinforce the OTHER end, so it wouldn't break off someday, too. I also packed some into the corners of the piece (using a toothpick) to reinforce some stress points, and filled in a couple of cracked areas from behind while I was at it. This was tedious, as the pieces are small, and you have to be careful not to add material to spots that need to clear certain parts. (Like the light bulbs for the marker beacon lights...) The following afternoon it was time for the big test -- could I actually drill this stuff without breaking the new "end" out completely? I first carefully removed the strapping tape, and was surprised when it came off of the new material rather easily. I then marked where the holes needed to go, chucked the piece on end into my drill press, and EVER so carefully lowered the spinning bit into the new plastic. You can imagine how relieved I was to find that it cut through just fine. The new J-B Weld plastic was just as strong (maybe stronger?) than the original part, and I quickly finished drilling both holes. It was a little spooky counter-sinking the holes for the screw heads, since it meant hitting the piece with a fairly large drill bit. Again, however, it held up to the drilling force just fine. Upon reassembly, however, I discovered that my new end was JUST a tad thicker than the original -- I had reinforced it a bit much. This didn't allow the faceplate to mount on the audio panel chassis properly, so, using the spinning bit in my drill press like a router, I carefully hogged out tiny bits of the new material at a time, until it fit perfectly. All that was left was the cosmetic touches. Using some flat black model paint (J-B weld dries to a light gray color), I painted the new material to match the original plastic. Since the repair is almost entirely on the side of the faceplate, it's nearly impossible to see the new piece, and -- after painting to match -- you can't see it at all. I reinstalled the unit today, and it fits, looks, and works as good as new. J-B weld is amazing stuff, and I'm $200 ahead because of it. |
#4
|
|||
|
|||
![]()
Now invest some of that money in a Dremel tool and I'd bet you'll be
able to literally sculpt your next J-B Weld project. Got one. It's a great tool, but the drill press gave me a solid, spinning cutting tool against which to push the piece, rather than the other way around. This difference gave me much more control over the cut. -- Jay Honeck Iowa City, IA Pathfinder N56993 www.AlexisParkInn.com "Your Aviation Destination" |
#5
|
|||
|
|||
![]()
Now it's time to fix all thos cracks in your interior plastic overlays
![]() used a similar type of plastic epoxy to fix my instrument panel plastic and it worked great. I also was able to "re-cover" my right yoke with Plasti-Dip and that too had great results. I was afraid that it would start peeling after a year or so but it's still holding strong. Not as cold to the touch as the powder-coated left yoke too. Marco "Jay Honeck" wrote in message news:kOjTb.76216$U%5.412616@attbi_s03... Now invest some of that money in a Dremel tool and I'd bet you'll be able to literally sculpt your next J-B Weld project. Got one. It's a great tool, but the drill press gave me a solid, spinning cutting tool against which to push the piece, rather than the other way around. This difference gave me much more control over the cut. -- Jay Honeck Iowa City, IA Pathfinder N56993 www.AlexisParkInn.com "Your Aviation Destination" Posted Via Usenet.com Premium Usenet Newsgroup Services ---------------------------------------------------------- ** SPEED ** RETENTION ** COMPLETION ** ANONYMITY ** ---------------------------------------------------------- http://www.usenet.com |
#6
|
|||
|
|||
![]()
Now it's time to fix all thos cracks in your interior plastic overlays
![]() Don't have any left! Actually, there is one cracked piece around the windshield which is not visible unless you stick your head up by the whisky compass. Every time I do that (like, once a year) it bugs me, so eventually I'll replace it... :-) -- Jay Honeck Iowa City, IA Pathfinder N56993 www.AlexisParkInn.com "Your Aviation Destination" |
Thread Tools | |
Display Modes | |
|
|
![]() |
||||
Thread | Thread Starter | Forum | Replies | Last Post |
Repairing Plastic Interior Parts of 40-year-old Aircraft | jls | Home Built | 6 | December 7th 04 10:04 PM |
FS: Revell Monogram "F-14A Tomcat" Plastic Model Kit (1:48 Scale) | J.R. Sinclair | Aviation Marketplace | 0 | August 16th 04 05:59 AM |
BrandNew-Vector Heavy Duty Plastic Construction Tape Dispenser 13 Peaces Left | [email protected] | Aviation Marketplace | 0 | April 29th 04 11:43 PM |
Repairing Plastic Instrument Panel Overlay | Jeff P | Owning | 22 | January 29th 04 06:42 PM |
replacing plastic panel overlay w/aluminum | Dave | Owning | 7 | January 10th 04 10:52 PM |