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#31
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#32
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There's a trick that I read about on the web for removing broken steel studs
from aluminum engine heads where you find a washer with the same interior diameter as the stud, use a TIG welder to weld the washer to the stud, then weld a nut to the washer. Use an impact wrench at the lowest setting to turn the stud out. Jim "David Lesher" wrote in message ... "pbc76049" writes: I had a real tough plug to pull once. I JB welded the allen wrench into the socket and it cane out with little fuss after massaging the case with a heat gun to 250f measured with my trusty IR temp gage......... This was my next suggestion. -- A host is a host from coast to & no one will talk to a host that's close........[v].(301) 56-LINUX Unless the host (that isn't close).........................pob 1433 is busy, hung or dead....................................20915-1433 |
#33
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I have done this...last ditch effort...ran the engine to warm, iced
the allen wrench/plug, (it was a "socket" allen wrench) twisted with a "T" handle to equalize torque... It came out... Heated the plug with a torch, the J-B let go, allen "socket" salvaged... Dave On Tue, 7 Nov 2006 09:12:37 -0600, "pbc76049" wrote: I had a real tough plug to pull once. I JB welded the allen wrench into the socket and it cane out with little fuss after massaging the case with a heat gun to 250f measured with my trusty IR temp gage......... |
#34
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I wouldn't reuse it.
"Dave" wrote in message ... I have done this...last ditch effort...ran the engine to warm, iced the allen wrench/plug, (it was a "socket" allen wrench) twisted with a "T" handle to equalize torque... It came out... Heated the plug with a torch, the J-B let go, allen "socket" salvaged... |
#35
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Well, tonight I'll finish cleaning up the install of the wiring harnesses,
EGT, & CHT probes and tackle the oil galley plug. I've already warned my A&P that he'll be expected to lead the way... and he's already warned me that it might not be a pleasant path. I'll report back with news of our adventure. Thanks for all the great advice, I'm sure that we'll put more than a little of it to use this evening. Jim |
#36
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On Thu, 9 Nov 2006 11:55:16 -0600, "Jim Burns"
wrote: Well, tonight I'll finish cleaning up the install of the wiring harnesses, EGT, & CHT probes and tackle the oil galley plug. I've already warned my A&P that he'll be expected to lead the way... and he's already warned me that it might not be a pleasant path. I'll report back with news of our adventure. Thanks for all the great advice, I'm sure that we'll put more than a little of it to use this evening. Jim Good luck Jim. z |
#37
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GOT IT!
Well, thanks to all of you for your great advice, here's how we approached it. Strip out 3/16" internal hex head as expected. Fit a 3/16" EZ out into the plug and we found that it bottomed out in the plug without gripping the sides. Ground about 1/4" off of the EZ out so it wouldn't bottom out and fit snug. Heat the dog **** out of the case with a propane torch and an electric heat gun, being sure to keep the heat moving and not burning the paint. Tapped the EZout into the plug. The EZ out I used had a 1/2" hex head, so we used a socket and ratchet to turn the EZ out. This helped us keep it square and apply pressure against it, driving it into the plug. As it tightened, we removed the socket, tapped the EZout in further, applied more heat, turned the EZ out a little more, more tapping, more heating, more turning slightly, more tapping.... finally we "thought" that something was giving... but we didn't know if it was the EZout or the plug, OR if the exterior portion of the plug had began to split! ![]() turning... YEP! bingo! Didn't have to drill... didn't have to pull the prop and the ring gear... whew! ![]() Thanks again for everybody's advice. Jim "zatatime" wrote in message news ![]() On Thu, 9 Nov 2006 11:55:16 -0600, "Jim Burns" wrote: Well, tonight I'll finish cleaning up the install of the wiring harnesses, EGT, & CHT probes and tackle the oil galley plug. I've already warned my A&P that he'll be expected to lead the way... and he's already warned me that it might not be a pleasant path. I'll report back with news of our adventure. Thanks for all the great advice, I'm sure that we'll put more than a little of it to use this evening. Jim Good luck Jim. z |
#38
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"Jim Burns" writes:
GOT IT! Well, thanks to all of you for your great advice, here's how we approached it. Bravo. [Too bad no one makes Torx head pipe plugs.] -- A host is a host from coast to & no one will talk to a host that's close........[v].(301) 56-LINUX Unless the host (that isn't close).........................pob 1433 is busy, hung or dead....................................20915-1433 |
#39
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![]() "Jim Burns" wrote in message ... GOT IT! Well, thanks to all of you for your great advice, here's how we approached it. Strip out 3/16" internal hex head as expected. Fit a 3/16" EZ out into the plug and we found that it bottomed out in the plug without gripping the sides. Ground about 1/4" off of the EZ out so it wouldn't bottom out and fit snug. Heat the dog **** out of the case with a propane torch and an electric heat gun, being sure to keep the heat moving and not burning the paint. Tapped the EZout into the plug. The EZ out I used had a 1/2" hex head, so we used a socket and ratchet to turn the EZ out. This helped us keep it square and apply pressure against it, driving it into the plug. As it tightened, we removed the socket, tapped the EZout in further, applied more heat, turned the EZ out a little more, more tapping, more heating, more turning slightly, more tapping.... finally we "thought" that something was giving... but we didn't know if it was the EZout or the plug, OR if the exterior portion of the plug had began to split! ![]() slightly... keep turning... YEP! bingo! Didn't have to drill... didn't have to pull the prop and the ring gear... whew! ![]() Thanks again for everybody's advice. Jim A follow-up question... Looking back, would it have been easier to pull the prop and ring gear in the first place? One thing that I hate is working in awkward and/or confined areas. That kind of thing seems to lead to stripped heads, busted knuckles, etc. I have a fixed pitch prop and with the cowl off, I can have the spinner, prop, and ring gear sitting on the hangar floor in 20 minutes or less. |
#40
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On Fri, 10 Nov 2006 23:12:56 -0600, "Jim Burns"
wrote: GOT IT! You must've felt like you won the lottery after it came out for you! Glad it worked out. z |
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