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#51
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Hudson River Opportunity
Tony
You are probably right. Was a long time ago. Think there was some discussion about snow or something on wing (long time holding after de-ice) and power setting pilot used and combination caused bird to not fly off normally in the snow storm on R/W length available? Is it just the American way for someone to risk his life to save individuals involved in any kind of a catastrophe? Big John Big John On Mon, 19 Jan 2009 10:51:31 -0500, TonyV wrote: brtlmj wrote: On Jan 18, 1:16 pm, Tech Support wrote: That accident was attributed to Pilot error as I remember. Tried to take off with snow or frost or ice on wings. Icing in the engines disabled some sensors, and the pilots thought they were developing much higher power than they really did. I recall reading that the accident was avoidable - had they recognized what was wrong and pushed the throttles forward... Shouldn't they have fire-walled the throttles regardless? I remember reading about a Shorts driver, caught in a micro-burst, who did just that - mandating an expensive engine hot section teardown. At the "inquest" he was asked why he run his engines up to 120% of their rated power. His answer was "I couldn't get any more". Getting back to the Air Florida crash, the NTSB, when listening to the cockpit voice recorder, immediately knew that the engines were not producing enough power simply by the sound. Tony V. |
#52
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Hudson River Opportunity
On Mon, 19 Jan 2009 08:39:02 -0800, Darryl Ramm wrote:
That sucker floated quite well if water was coming in the rear door and the ditch switch was not activated. A report I saw today said the rear door was not opened. The cabin crew realized it was partly underwater and stopped a passenger from trying to open it. -- martin@ | Martin Gregorie gregorie. | Essex, UK org | |
#53
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Hudson River Opportunity
On Jan 19, 9:32*am, Martin Gregorie
wrote: On Mon, 19 Jan 2009 08:39:02 -0800, Darryl Ramm wrote: That sucker floated quite well if water was coming in the rear door and the ditch switch was not activated. A report I saw today said the rear door was not opened. The cabin crew realized it was partly underwater and stopped a passenger from trying to open it. -- martin@ * | Martin Gregorie gregorie. | Essex, UK org * * * | There is at least one media report saying that a passenger was able to partially open a rear door. There is also conflicting reports about wether flight attendants tried to open the rear doors themselves first or had asked passengers to do this before realizing this was a bad idea. There are reports of passengers talking about water in the rear of the plane fairly quickly. A door may have actually been partially opened or this water from other sources may have made people think a door was opened. I won't provide links here, it's easily googleable. We will have to wait until clearer information to (hopefully) know for sure, the NTSB report will be interesting reading. Darryl |
#54
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Hudson River Opportunity
TonyV wrote:
(Air Florida accident) Icing in the engines disabled some sensors, and the pilots thought they were developing much higher power than they really did. I recall reading that the accident was avoidable - had they recognized what was wrong and pushed the throttles forward... I read that report not long ago, so I happen to remember the details: Mistake 1: They used reverse thrust for push-back on ground. This was against a clear company policy. Doing so, they sucked a lot of snow into the engines. Mistake 2: They forgot to engage the de-ice system of the engines. This resulted in clogged probes, resulting in wrong power readings. (The instruments showed much more power than the engines actually delivered.) Mistake 3: The copilot realized during the take-off run that there was not enough power. The captain ignored his warnings and continued the take-off. He also ignored the fact that the take-off run needed 800 meters more than expected. |
#55
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Hudson River Opportunity
On Jan 17, 7:11*am, Andy wrote:
Yes A320 has a RAT and it automatically deploys on loss of AC bus 1 and 2 which would happen if both engines lost power (and the APU was not running). * Preliminary reports indicate the APU was running. The APU manufacturer has even received a thank you message from one passenger. I cannot see a deployed RAT in any of the salvage photos. So either engines at or above idle, or the APU, would have been able to provide normal electrical and hydraulic services. Andy |
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