"569" wrote in message
oups.com...
snip
alternator had seized, and the belt was
still attached. The black smoke and burning smell was the rubber from
the belt. The RPM drop may have been cause by the belt briefly
cinching up. It also explained the low voltage light as well.
I went home and enjoyed a few cold beers. The worst part was not
knowing the problem or what was going to happen next. The plane was
flying the next morning, and me, in the same plane the very next week.
BRAVO!!
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